FINANCE COMMITTEE
MEETING
OCTOBER 11,
2005
The meeting was called to
order by Chairman Fogt at 5:35 p.m.
MEMBERS PRESENT: Nevin Taylor, Dan Fogt, Ed
Pleasant
OTHERS PRESENT: Dick Noland
AGENDA:
1)
Sewer Rate
Increase
2)
A
summary of Mr. Noland’s presentation was given to all of
Council.
Mr. Noland addressed the
Committee. He talked to OEPA and
made arrangements to go down and look at the application, which was put together
by Malcolm Pirnie and City of
Mr. Noland reviewed all
alternatives looked at by Marysville.
He
is here as a rate payer. Currently
on the county water system, but after the first of the year, will be on the City
system. He is also in the pathway
of Marysville for annexation.
Mr. Noland noted while
talking to OEPA, he learned there were three non-degradation systems for smaller
flows in
He
made the following points: 1) Water
quality of
This existing plant, most
of it is since 1984, is about half the capacity or since 1990, and the
headworks, a major part, is only five years old. He noted in the report that the existing
facility was old and needed a lot of repair. Mr. Noland feels this is not
old.
Would like to have seen
more specifics of just what is wrong with the plant and what it would take to
put it back into good working order.
Would like to see what it would take to make it last another 10-15
years.
The plant certainly has
some value in it. The County and
the City do need additional capacity.
Seems simple to separate
part of the system and take it to another plant.
Learned from Marysville
records, inflow and infiltration is a big problem. Removing rainfall inflow and in some
cases infiltration, is the most economic means of getting more plant
capacity.
The full cost of required
sewer systems and treatment facilities in new undeveloped areas some distance
from municipal sewers should be a part of the total cost of serving these newly
developed areas. Costs and risks
associated with these developments should be totally upon the developers and not
on the Marysville existing sewer customers. Mr. Pleasant said this committee agreed
with Mr. Noland on this issue.
Improvements to the
existing Marysville sewer system, by eliminating pump stations, can best be
absorbed by the existing and future rate payers if they are phased over the longest possible period of time.
It
appears that the existing force main from the Scotts pump station and bowling
alley pump station to the existing wastewater treatment plant could possibly be
used by reversing the flow to take the flow from these areas to the new
treatment plant located on Beecher Gamble Road.
Some modifications to the
pump stations and additional force main would be required to facilitate this
alternative.
Alternative “C” for
minimizing the lowering of the
Main
points:
q
Construct a new 2 MGPD at
the new site south of the City.
q
Take the existing and
future ______ flows up to their capacity from the bowling alley pump station
back to the new plant.
q
Continue to remove I & I from existing system and the County
system.
q
Continue to use the
existing 4 MPGD plant for 10-15 years and use the existing County facility to
its capacity, and then require new development in Millcreek and
If
you take the existing flows back to those pump stations and pump it into the
plant, this permits the longer time of phasing out the
existing plant and constructing major interceptors. Permits more time to continue removing
I & I from existing City and County collection
systems. Permits spreading major
costs of a larger new plant and major interceptors to eliminate pump stations
over a longer period of time, thus reducing rate increases right now. Provides for an
incentive to use non-degradation system in open, undeveloped areas like between
Marysville and
Disadvantage is requiring
the operation of two plants.
Economics are in favor of this alternative. Would need two Class 4
operators. Requires an additional force main between Scotts pump station and
the new plant. Requires some
modifications at the bowling alley pump station and the Scott pump station. Requires the continued
operation of the existing pump station. To do it properly would require some time
and funding for a detailed evaluation of this alternative and a comparison of
capital and operating cost.
Estimated cost of the new
force main to be about about $1M.
Modified at the force main
at bowling alley pump station estimated $500,000.
Modifications of the pump
station at Scotts estimated at $500,000.
Construction of new 2 MGPD,
using Malcolm Pirnie’s way of estimating the treatment plant, estimates
$15M. With a 2.0 MGPD plant, would
not need a new administration building.
Don’t need a new equipment and maintenance building at the new
plant. Don’t need a major new headworks.
Cost to rehab existing
plant to last 10-15 years could be done for 1/3 the cost of building a new
one.
Mr. Fogt noted the anaerobic digester was replaced to help
eliminate the odor. There is no good way to clean out the old system without
stopping the flow, and we don’t have the capacity to stop the flow. The headworks project was designed
wrong, according to Malcolm Pirnie.
Mr. Pleasant encouraged any
and all input, but not sure what would be done with it. All this information will be attached to
the minutes for public information.
Mr. Noland said estimated
cost for this Alternative C is $31,000,000. He would need to talk to various
individuals and visit the plant again to firm up numbers. This is workable in theory. Need to work out the details to confirm
or show it doesn’t. The City has
not wasted any money thus far. It
will not affect or impact the City or City residents. The area south of City in Jerome and
Mr. Noland will give this
alternative at the EPA Hearing.
Regarding annexation, Mr.
Pleasant encouraged
3)
Stormwater
Fees
Need to create legislation
to continue stormwater fees for 2006 and possibly 3 years out. Mr. Fogt recommended continuing with the
fees currently in place. Mr.
Pleasant agreed. Fees will continue
through 2008.
Meeting
adjourned.